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Group assignment
I did the group assignment during the lecture with Toni Kyllönen and our instructor was Behnaz Norouzi. Epilog laser controller uses percentages for Speed and Power. It is weird that the frequency doesn't have any kind of unit in the controller. I thought that I should have tested if the controller would accept a higher number than 100, even when I tested the effect of the frequency the highest number I used was 100.General things about laser cutter
Basic setting on the laser control
You use the laser from the computer like a printer, you choose to print and then you select the preferences to get to the laser controls that are shown above. In the General tab most important settings are the job type, and settings under the Raster and Vector settings. From advanced tab you can load some pre-sets for different kind of materials. I find that the vector settings for cutting are usually a bit too optimistic and you need to lower the speed or raise the power to get a good cut. In the Color Mapping tab you can specify the laser to use different settings for different colors.
Focus tool on the laser head On the laser you can jog the head close to the area you are going to work on by selecting the jog function and using the joystick to move the head. You can turn on the position laser on by clicking the red star thing on the control panel. By clicking the joystick, you set the new origin of the job. Then you can set the focus by using the focus tool and selecting the focus function. You put the focus tool on the laser head and you want to raise or lower the laser bed in a way that the focus tool is lightly touching the material. You can change the speed that the bed moves by flicking the joystick to the left, the speed is indicated by diamond symbols. Once you are happy with the focus height you confirm it by clicking the joystick. Now you can just check that exhaust and air is on and confirm that you are going to do the right job. Then just press GO and keep a close eye on the process in case there is problems.
Cutting; speed & power
Cuts with different power and speed settings Engraving; speed, power & DPI
Engraving with different power, speed and DPI settings Focus
Cutting and engraving in focus, above the focus and below the focus Cutting; frequency
Cutting with different frequencys Kerf
Kerf testing pieces that I made Kerf in different axis in 3 mm MDF Kerf in different axis in 3 mm PMMA. The zero marks the origin of the laser.
I almost feel that it is waste of time trying to make a good fit in solid materials if the kerf can really be 4 times larger in one axis than the other. The off axis kerf would then be just anyones quess and the design would be really complicated to calculate all the kerfs in the different directions.Joint clearance
Joint clearance tool that I made. Test piece is in the slot that is thickness - 0,05 mm wide Downloads
Download corrected_kerf.svg
Download Group_Test_Focus.svg
Download Group_Test_Kerf.svg
Download Group_Test_Raster.svg
Download Group_Test_Vector.svg
Download parametric-joint-clearance.f3d -
Vinyl cutter
Vinyl cutter. The lever is in the top left and the control panel on the right. The vinyl cutter in Fab Lab Oulu is Roland CAMM-1 GS-24. When you start the vinyl cutter, you can select the material type, roll, edge or piece. Roll is obviusly the big roll, I think you can use two different widths of rolls. Edge detects only the width of the material while the piece option detects both, width and height. You can load the different materials in to the vinyl cutter by pushing the lever on the right. you need to adjust the rollers depending of the width of your material. The rollers need to be where white marks are on the top. After loading the material and adjusting the rollers you can close the rollers by pulling the lever. you can also adjust the origin in the X-direction while the rollers are open just by moving the cutting gantry and after that holding the origin button to set the new origin. I am not sure if you can adjust the origin in the Y-direction, I should have asked. (
EDIT:
Apparently you can move the cutting carriage with the arrow buttons on the control panel, this way you can move cutting origin in both directions.) You can bring up the reset settings menu by pressing the menu button twice. On the bottom of the control panel you can adjust the cutting pressure by the slider. You can control the vinyl cutter straigth from Inkscape. You want to select the Roland cutter from the printing menu and got to printing preferences. There you need to selectGet from the machine
in the Cutting Area settings. Sometimes the machine doesn't actually make the cut and this can be fixed with selecting theRotate 90deg
option. If you need the cut in the certain orientation you can prerotate the design in Inkscape.
In the lecture when we tried different cutting pressures it seemed like lighter pressure might have shredded the design a bit more. From the back of the cuts you could see that the higher pressure cut more in to the backing. The material we used was pretty durable and it didn't seemed to need really precise settings. We also tried to use the cutStudio but weren't succesful. I am pretty sure that it had worked before by just copying and pasting the design from the Inkscape but now we didn't get it the work.
I had made this design that I wanted to cut a couple of stickers. I had made this design years ago in Inkscape so I decided to just scale it to right size which was 50 mm wide. I didn't want to use a full roll, so I dig through the scrap bin and found a suitable matte black vinyl piece from there. I straightened a bit, loaded it in the machine and selected the piece option from the menu. I used Inkscape to print the design. I selected the roland printer and chose theGet from the machine
in the Cutting Area settings. I printed the design but nothing happened. I then selected theRotate 90deg
option and printed it again. This time it cut the design. I moved the origin and cut two stickers more. Weeding them was easy because the design was pretty simple and nothing was relly small. Also the material was quite good. Previously I have had problems with weeding because the material I used had such a strong glue that even though I cut with the full pressure, the glue would start instanly bonding again and fused the cut parts together. I then stick some tranfer tape to weeded stickers. I then glued one in my phone, one in my laptop and one is just waiting for a right application.Downloads
Download tarra.svg -
Parametric design
I made the first version of the design in fusion 360 pretty quickly. I started with a center rectangle and added equality constraints to the sides. I added the parameterxy
to describe the width and height of the part. I added fillets and used formulaxy/5
to calculate the radius. I made a slot in the rectangle and used constraints to stay center of the side. I wanted the width of the slot to be thicknessz
after the cutting. I made new paramaterkerf
and gave it a just some near enough value because we hadn't measured the kerf oursleves yet. Now I could calculate the sloth width withz-kerf
, I called this parameterinternal
.
When thinking about slot depth I realized that thexy
wouldn't be the real parts dimensions. I made a new paramater calledxy_real
and used it to calculate xyxy=xy_real+kerf
. I also changed thez
parameter name toz_real
just to keep somewhat regular naming. I wanted that, if you would put three pieces together there woulnd't be gap between the two edge ones. Later I realized that this would prevent the slotting three different pieces in 90° angle but at the moment I carried on. I figured that theslot_depth
should bexy_real / 4 - kerf
. Later I changed the slot_depth to leave a gap that would be a size of the material thickness. So mysloth_depth
was( xy_real / 4 ) - ( z_real / 4 ) - kerf
. I found out that even this was wrong because I already had the kerf included because the sloth depth was measured from the edge of the part and that already had half of the kerf included. Half the kerf is all I need because the other slotting part has the second half. I realized this when I was playing around and trying to use just the offset tool to add the kerf. So I made a new design that had the original sketch with dimensions that didn't include kerf. Then I added some clearance to the slot depth. I scaled that to material thickness because I thought that if the material is thicker, it would be harder to cut to precise dimensions. So now thesloth_depth
wasxy_real / 4 - z_real / 4 - 0.05 * z_real
.
Now I could use circular pattern to copy the slot to four sides and just trim the extra lines. Then I just extruded the part usingz_real
as a parameter. I added the values that you are expected to change to favorites so I wouldn't accidentally change the formulas. You can see the heavily constrained sketch, part, and parameters below.After this I decided to use the offset tool to model the kerf. In the picture at right you can see that I made the original shape I want after laser cutting as construction lines. Here I made the the outline and made it 20 times bigger than it should so you could see the construction lines and the offset line at the same time. In the real design the
offset
iskerf / 2
. Fusion 360 doesen't have a chamfer tool in the sketches so I extruded the part to thicknessz_real
. I added the chamfers to slots corners and made a new parameterchamfer
whit the formula asxy_real / 40
.
I also had made a quick version with 8 slots. I made this one before discovering the easier offset method. I made a quick fix for this part because in the first version if you would put two parts next to each other, they would hit each other before hitting the bottom of the slot. I just scaled the partsxy
with the formulaxy_real * 1.5 + kerf
. I know I could have made better formula with all the dimensions to scale it more intelligently, but I just wanted to get it working.Cutting the parts
I spent quite a lot of time just fine tuning the parameters and making test cuts. After I had measured the kerf in acrylic, I only adjusted the thickness of the part in parameters in fusion 360. I also changed the design to have more chamfer. It was quite hard to get a good fit because when I had perfect fit in Y-direction, fit in the X-direction was too tight. I was using some scrap piece for fine tuning and after I had good fit I realized that I didn't have enough room for the "production" run. So I had to change the acrylic sheet and of course the new scrap sheet was slightly thicker so I had to do the fine tuning again. On the left you can see that the new sheet was thicker and when I tried to force the parts together, even in the looser Y-direction, the acrylic formed cracks. This reminded me that I could have added some fillets or chamfers to distribute the load better. At the Fab Lab I thought that I got the fit pretty close but at the home when inspecting them in greater detail, I ended up with a too loose fit. You could still use the parts for building, here is a snake and some modern architecture.
If I had made this assignment out of cardboard, it would have been easier. Cardboard would have had some springeness and I could have used a bit too tight fit with chamfers and it would have worked great. I could have used MDF but handling the cut parts with the fine wood dust gives me allergies.
Downloads
Download multiple-slots.f3d
Download multiple-slots.stl
Download simple-block.f3d
Download simple-block.stl
Download multi.pdf
Download simple.pdf
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Final project
Shaper Utilities plugin for Fusion 360 All the correct settings done Cover bolted to the case Button bracket in Inkscape Bottom is bended with heat gun. The rest are bended with laser, top one is the last one that I tried. During the summer I had also told Akseli about LaserOrigami and he had tried. I wanted to try it myself and asked his advice. Sadly he didn't remember any of the settings he had used so I just started with the settings mentioned in the LaserOrigami website.
Slot You can see from the photos above that I didn't quite get the setting completely right, there was still some boiling/over heating of the acrylic. In the end I used 30% speed and 10% power and I had 50 lines over each other and just stopped the machine when the piece looked like it could be bent by hand.
In the end I ended up using the piece that was bent with the heat gun but the LaserOrigami technique is worth a try in a future.
Downloads for Final Project
Download cover.svg
Download buttonBracket.svg